|
|


19th February 2008 session 9 Well today was certainly a learning experience! Got the angle for setting the topside over for internal screw cutting completely wrong! Failed to cut the cavity with the 3/4" end mill with any sort of success and finally, if this had been the 'proper' crankcase it would have been successfully turned into scrap! So those were the positives......What I did achieve however was to realise something was wrong with the screw cutting and saved my sanity for another day. All of which certainly adds to my 'experience' as a novice model engineer and that is what it is all about is it not. So I started firstly by trying to set up the crankcase to use the 3/4" end mill in a different way to Ron Chernich. Guess what, he has the best methods! I did not feel that the accuracy I could get by moving between the lathe, the mill and back to the lathe again would work. So I reset the practice blank back in the 4 jaw chuck and decided I would bore out the remaining width and depth instead of continuing with the end mill in the monstrous MT2/MT3 extension. I could see the adaptor being useful in a milling situation but I feel that in the lathe its length would not allow the accuracy I think is needed. More experienced engineers may well put me right on this......anyway I decided to bite the bullet and get a MT2 collet holder after all. I will need to use this facility many times I would guess in the future. I have a set of ER25 collets recently purchased so getting an MT2 holder makes sense. Its just that I am tight sometimes and in this instance that has caused me to spend more! Boring out the cavity to the required dimensions went well. It took a little while to sort out what was required for the deeper recess further inside the crankcase, referring often to the plans as well as Ron's description. This time was not down to a lack of clarity on Ron's part, more to my concentration level's. Anyway I got there in the end and achieved the correct dimensions for the cavity( see photo 1 on the right) but only after changing boring tools. The first one would not give enough clearance for the recess so I changed it for a better tool (photo2 on the right) and thereafter had no problems. After reaming the shaft hole I could no longer delay the dreaded internal screw cutting for the back plate. So checking again (and again!) the required angle to set the top slide over to (29.5°) I went to unlock the top slide but it wouldn't move! I thought I was being clever by fitting the digital readout on to the top slide. Indeed it worked very well earlier. but my method of securing it would not allow the top slide to move. So it had to come off (and I will have to have a rethink when it comes time to refit it). Anyhow whilst I could see the threads starting to form they did not appear to be getting deeper and I was more than a little disappointed (photo 3 on the left). So what if anything had gone wrong? I would have to re-read the books on screw cutting. I also had a look at the photo's in the magazine article and Ron's certainly looked better!. Its just a good job I decided to keep going with the defective blank. Something I think I will do again with the next suitable project. So quite an eventful morning really. On retiring to the bungalow armed with various books and my Jose F. Rodriguez video's, (worth their weight in gold to the novice! - click here for link to buy, ). Well I know where I went wrong now. I thought that since my top slide sits on a graduated scale marked in degree's I needed to set it to 29.5. But no, the angle relates to the top slide setting against the cross slide. Having the top slide set as I did I was not increasing the depth of the screw as I was pushing it across the x axis....... so now I know. I think I will have another go on a blank piece of aluminium and not the crankcase yet. I feel I need to get this right first as it is a very important area to ensure the engine runs! Quite an eventful morning as I said. I am not disappointed as there were many good learning points and no major damage! Time spent today 3 hours 30 minutes. Total to date 16 hours. 00 minutes. |
photo 1 |
photo 2 |
photo 3 |
Mills Crankcase session 9 - updated 1st December 2008 |
www.mikes-models.com |