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mikes-models.com |
mikes-models.com |
5th March 2008 session 15a Well following an email to Ron Chernich I decided to give the milling of the crankcase a go. I spent 45 minutes setting the crankcase up on the angle plate [photo a] using an electronic edge finder [photo b] This ensured the case was level in all planes (sorry about the pun!). Ron stresses that you must be careful when breaking through with the drill, so as not to drill into the datum plug. So I was particularly careful with the drilling and decided I could indeed be a bit clever here…..so to prove how clever I am, I drilled into the plug! I found setting up the crankcase for milling, whilst time consuming, didn’t cause many problems. I decided also to pack out underneath the crankcase in case any tendency to push down occurred when first drilling. A bit belts and braces really…so how did I go wrong and drill the datum plug? Well I thought it would be quite clever to drill down so far with the first small drill, before opening up the hole with increasingly bigger drills. I then changed to the next drill size up and drilled down to the same depth, guided by my digital readout. I thought that if I then reverted back to the smaller drill, I could fill the resulting hole with cutting fluid and as I broke through, the fluid would drain, and I could then set the digital readout to zero, thereby making it safe for all other drills and the boring bar. This plan seemed to work and I was pleased when the hole drained. For some reason (called stupidity!) I looked into the hole with an angled mirror to check that all was well and saw that I had broken through, so instead of setting the readout to zero, I continued to drill down! Why? Just mindlessness! I instantly knew that I had gone too far, and the realisation that I had made a big mistake dawned heavily on me……however, when looking again into the drilled hole I couldn’t be sure whether I had damaged the plug or no, but how could I tell without disturbing the crankcase? It took a while, thinking what I could do, but without an endoscope there was no way out of it. The crankcase would have to come off, loosing all my settings into the bargain! However, I hadn’t got past the stage whereby all would be lost, although it would be a pain in the £$%. So oft it jolly well came. And sure enough, my worst fears were realised. I had drilled into the steel plug [photo c]. Now what? I would have to make a new plug and that would really be a problem, one that I didn’t rally want. I went and made a cup of tea and had another think. The plug was there so I could measure the amount of material to skim off the top. As Ron so ably explained in his email to me, this was a critical measurement, and a couple of thou out, would mean a big, big difference in the engines starting and running. Then it came to me that if I filled the hole flush, that would be ok. I had some ‘plastic metal’ a two part mix. If I filled the hole and left it overnight to cure than with careful sanding, I should be able to recover the situation, as long as it is flush. So I mixed up a little of the filler and left it to cure overnight [photo 26], so it should be ready for the next session. I will test the results with a dial gauge just to be sure it is acceptable. If not, it’s another plug to make. Not a disaster, but it stopped me finishing this part of the job today. So all in all, not a good day…..So I started on making the switch box for the Myford refurbishment .............. Time spent today 1 hour 30 minutes. Total to date 32 hours. |
photo a |
photo b |
mills crankcase session 15a |
photo c |
photo d |