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mikes-models.com |
mikes-models.com |
Candlestick adaptation. I was asked recently if I could help one of my brothers with a problem he had with silver candlesticks (worth a lot of money). His problem was that he had to replace the bases on which this pair stood, as one was damaged and had been repaired (but not to a satisfactory standard). He went and sourced a nice pair of replacement bases, but herein laid the problem. The securing mechanism for the candlestick to the bases was via a short brass rod that was secured into the base, in such a way as to make its removal a none starter. The problem to be solved as I saw it was to some how lengthen the securing method through the existing holes in the new bases and secure them so that the base stood flat. The solution I chose to adopt was to make an extension tube with threaded ends. One, to suit the brass rod, and the second, to suit a new screw, yet to be made. Because of the value of these candlesticks, there had to be a ‘quality’ solution, especially as whilst they would not be prominent, the extension pieces would be seen. Because using silver was not an option to me I decided on stainless steel. Its use had many attractions to me, firstly it would not corrode. Secondly, it was extremely durable. Thirdly, I have never machined stainless steel before, so I would add to my experience and finally because I had just bought a few oddments from eBay! Sorted. The machining followed fairly late on in the process. Firstly I had to work out the length of the extension pieces, the diameter of the screws to be made, the thread already on the brass rod and see whether I had any taps to match the existing brass rod. And all that I was to do could not affect the candlesticks safe untouched return to my brother if I couldn’t succeed. The answer to the question of thread size and whether I had a matching tap was soon answered. Nope. Ok, so I therefore had to see what I could re thread the brass rod too (and destroy my ability to return untouched!). As luck would have it a 3mm die would cut a sufficiently deep thread to make it possible to continue. Also if things didn’t work out I could easily make a fitting for the new threads so I decided to take the plunge cut the threads. Because these candlestick are so gorgeous and knowing me(!) I wrapped them in cloth then bubble wrap save for the bases showing. I also cleared an area where I could place them out of harms (and mine) way. I then cut the threads on the brass rod using the 3 mm die but it would only go down to about two thirds of the rod because of obstructions from the candlesticks feet. So when I made the extension pieces I would have to allow a clearance diameter for the portion uncut. The measurements of how long, what diameter etc. to use went on and on with me repeatedly checking and rechecking but finally I arrived at a set of dimensions and finding suitable stainless steel form my scrap box, got to work. Because I was dealing in small pieces I decided to uncover the Myford ML10 from under its dustcoat as it would be nice to use it again after the work I am doing on the large Chinese lathe (Turner 280GV). Also the Turner 280GV lathe held the crankcase of my Mills 1.3cc project in its 4 jaw chuck. And what a nice lathe the ML10 is. Its construction, quality and ‘feel’ are much better than the big lathe, but that has other advantages over the little ML10. I have, in the very recent past, considered selling the ML10 but I now realise this would be a big mistake. So it will stay with me, for similar ‘little’ jobs. Now the ‘easy ‘part started. I chucked the chosen diameter stainless steel rod and parted two pieces off to length. I then centre drilled one of the cut off pieces, then drilled out to suit a 3mm tap. This tap was held in the tailstock chuck and using cutting oil I tapped the tube for its length. I then reversed the piece and drilled the clearance hole for the correct distance. After a trial fit which seemed ok, and more importantly, in keeping (what could be seen) I made the second tube in exactly the same way. Trying this second extension piece onto its candlestick then putting the base in place I found out my first minor mistake. Whilst my two pieces were identical the candlesticks and bases were not! However because on new extension piece was too big, rather than too small, it didn’t need me to make a third! Next I started on the two stainless steel screws to match. Because of their small size (3mm thread) I decided to use the live centre in the tailstock to give support to the new screw and turned down the diameter of the rod until the required size was achieved. Leaving the larger diameter which would form the head, nearest the chuck. When sufficient material had been removed I slid back the tailstock holding the live centre and gently cut off the end of the screw blank, to size. Next, I switched off the lathe and removed the plug so I could use it safely when cutting the 3 mm thread. Finally moving a little more of the rod out from the 3 jaw chuck, I parted off the screw to suit the head width required. I carried out the same actions as described above for the second screw. Now it only remained for me to produce two stainless steel washers to match the screw head size and the diameter of the recessed base hole. This is a fairly simple task of producing the right diameter from available stock and drilling a clearance hole for the 3mm diameter screw, finally parting off two washers. So I now had the two extension pieces, matching screws and washers all made from stainless steel. All that remained was for me to make a slot cut in the screw heads to allow a screwdriver to be used when tightening the whole thing up. In the past I have been disappointed with the cutting of slots for screws I have made by using a small hacksaw for the job. And I didn’t want the screws to let the job down so I had a rethink. Eventually (all right a tea break!) I decided to give the proxxon a go using a small diamond cutting disk. All I can say is it was I found it a lot easier and giving a more accurate finish than my previous methods (it may be different for others. I don’t know). Now, when coming to fit the all the pieces together, all I had to do was make a small adjustment to the length of one of the screws, and they then tightened up nice and snug. When machining with stainless steel I was pleasantly surprised when my apprehensions proved unfounded. I have learnt that at least. The main thing though is whether the ‘customer’ was happy? I am pleased to say he was and when offering to pay for the’ job’ for the first time ever I said yes! My price would be a new scribe, which he duly purchased and now has pride of place in my pocket. So every time I use it I will be reminded of my first ‘paying job’. I found this ‘small’ job very satisfying because my skill base increased, I helped to provide a solution to making the candlesticks ‘nicer’ (not the extension pieces!!! The new bases!!!) and got more satisfaction than when doing my own projects! ----0000----0000---- ----0000----0000---- candlestick adaptation |
Candlestick repair |
Stainless steel screw prior to threading |
Base with new extension components |
finished piece fitted - a glimpse through the feet. |